liveforphysics wrote:I wouldnt even show up for an electric vs electric race. They are all my friends, I cant get in kill-mode or even motivated to race them. When its electrics racing gas bikes head to head, I go nuts for it and cant get enough, and no price is too much to pay for the experience.
There's nothing like a particularly smelly two stroke to bring the competitive "red mist" on- or that guy in front of you with on the little scooter and the super obnoxious plumber's crack hanging out! (If you were racing you know exactly what I'm talking about!)
I have to say I had a most excellent time at the race on Saturday, thank everyone for ignoring the economic arguments against it and COMING OUT TO THE RACE!
Here's the only media I have worth sharing- some onboard video of the partial race lap during which the motor died on PaulD's old bike. The video is a little long and uncut, check the description on Youtube for a "random access directory" to the important bits.
For the record, here's the short version of "outcome of Acuteaero's race weekend": Installed a 12fet Lyen controller on Thursday, set up with four shunts to solve "cutting out problem" viewtopic.php?f=2&t=16910. It was good for about six practice laps on Friday before shedding some solder off the board and blowing some fets (3077 fets- didn't have any replacements) It may well have lasted longer with a lower current limit. Borrowed Farfle's beefed up 24fet on Saturday morning and wired it in- set the battery limit reasonably low but the "phase current limit" far too high in the software- the motor heated up fast with low-speed acceleration and shorted a phase before the end of one race lap.
My other bike, named "the shortbus" is a BMX cruiser with a HS motor, add on wheelbase lengthening dropouts, 17" moped wheels and a suspension fork- it was fun to ride and reliable for dozens of laps- I low-sided it in one heat (why did I forget to wear gloves!), then my friend low-sided it in the same turn in another race... the bike was fine. It suffered mainly from a lack of refinement that matched the hurried nature of its construction- the brakes were bad to start and only got worse, and the fork (bought used on ebay...) obviously needs to be rebuilt- as well the original BMX bars are too short to actually fit a brake lever, throttle and hand grip on. I hope to get all these issues sorted out soon.
The Kokam LiPo packs I built for the race performed great- kind of a trial by fire as I didn't have time to thoroughly test them. I'll post photos of them in a different thread soon. Charging via Prius worked awesome. Only downside was that the big gas genset was running most of the time anyways! On friday before everyone else arrived I was charging in pure silence- with the prius engine running at idle only about 1/4 of the time! It was like magic! Even with all the charging and driving around at 75 mph I still got 40+mpg on the tank. (/end obnoxious prius fanboy session)
I'm a bit disappointed that I was not able to realize a better result with PaulD's bike- It's a beautiful machine and a temperamental beast. My failures also underline the meaning of Paul's success with the bike. He is truly a very capable dude. Of the many who have experimented with the RC motors on the forum few have stuck with them- I can understand why. The failures at this event are instructive to me though, I will continue reading on the forum about the success and failure of others with these motors and get set up better for next time. It's worth it
Again. I had a great time at the event, thanks to all of you who came and participated. It was great to meet some people I hadn't met before, and to hang out and be a part of the camaraderie. Looking forward to seeing you all again at the remaining events this year!






















