cal3thousand
10 MW
BUSTED:
So on the very last leg of my wife's long overdue bike build, I plugged the CA-DP wire into the Hall connector of the motor accidentally. Yes, I know the controller has a 6 pin JST and a hall should only have 5. But on this motor, a temp sensor has been installed by the factory and another wire comes out, so I put a 6 pin on there. (Apparently, I wasn't the only person to have made the same mistake http://endless-sphere.com/forums/viewtopic.php?f=2&t=31775)
The motor would not run and just made a noise like it wanted to run. Holding the wheel and pushing it backwards slightly and hitting throttle made the motor jump a tiny bit and then nothing. Per the other thread's conclusion, I knew it was the halls.
Having never done this before, I contemplated everything from swapping the motor to a HS3525 I have on had to sourcing a new stator for the MAC. But I'm cheap, so I figured I could fix it.
I tested the halls with a DMM while spinning the MAC backwards and 2 of the halls were showing nearly 5v and never dropped. Having some hall sensors on hand, I decided to give it a try. Did my best to remove the epoxy and not damage the windings with a heat gun and pick. Cleaned off the PCB, soldered 3 new halls onto it. (I didn't know which order to do it and thought this would give it the best alignment). Then I glued everything down with DP420 and waited for it to dry. Reassembled the motor to test.
REPLACED:
Now, I get a growling noise from the motor, but it doesn't turn. I made sure to test the PCB traces to the connector end for continuity on each leg. But I also reused the capacitor from the PCB without thinking. So I have a big suspicion that this is the culprit. I haven't tested the halls on the motor as it was getting late. Will do this tonight.
STILL NEED HELP:
Do you think I goofed by not replacing the cap? Or could it be a hall alignment issue? (I'm not sure I had them where they were supposed go exactly since the epoxy made it hard to precisely tell). I know that I need to do some more testing tonight (Got too late last night to finish), but I wanted to see if anyone had a good answers or tips based on experience so I can go back with a more focused attack.
Here's some photos of the situation: ( I know we love photos )
Before the repair attempt (notice the cap(?) on there) :
The halls are in place, trying out alignment, about to solder
Traces/wiring tested for continuity, everything glued down
So on the very last leg of my wife's long overdue bike build, I plugged the CA-DP wire into the Hall connector of the motor accidentally. Yes, I know the controller has a 6 pin JST and a hall should only have 5. But on this motor, a temp sensor has been installed by the factory and another wire comes out, so I put a 6 pin on there. (Apparently, I wasn't the only person to have made the same mistake http://endless-sphere.com/forums/viewtopic.php?f=2&t=31775)
The motor would not run and just made a noise like it wanted to run. Holding the wheel and pushing it backwards slightly and hitting throttle made the motor jump a tiny bit and then nothing. Per the other thread's conclusion, I knew it was the halls.
Having never done this before, I contemplated everything from swapping the motor to a HS3525 I have on had to sourcing a new stator for the MAC. But I'm cheap, so I figured I could fix it.
I tested the halls with a DMM while spinning the MAC backwards and 2 of the halls were showing nearly 5v and never dropped. Having some hall sensors on hand, I decided to give it a try. Did my best to remove the epoxy and not damage the windings with a heat gun and pick. Cleaned off the PCB, soldered 3 new halls onto it. (I didn't know which order to do it and thought this would give it the best alignment). Then I glued everything down with DP420 and waited for it to dry. Reassembled the motor to test.
REPLACED:
Now, I get a growling noise from the motor, but it doesn't turn. I made sure to test the PCB traces to the connector end for continuity on each leg. But I also reused the capacitor from the PCB without thinking. So I have a big suspicion that this is the culprit. I haven't tested the halls on the motor as it was getting late. Will do this tonight.
STILL NEED HELP:
Do you think I goofed by not replacing the cap? Or could it be a hall alignment issue? (I'm not sure I had them where they were supposed go exactly since the epoxy made it hard to precisely tell). I know that I need to do some more testing tonight (Got too late last night to finish), but I wanted to see if anyone had a good answers or tips based on experience so I can go back with a more focused attack.
Here's some photos of the situation: ( I know we love photos )
Before the repair attempt (notice the cap(?) on there) :
The halls are in place, trying out alignment, about to solder
Traces/wiring tested for continuity, everything glued down