Hi!
I'm building a commuter bike with q100c motor and a Chinese 17 amp controller with self learning procedure. The self learning procedure was not working for me. The engine always rotated backwards, but on the throttle it was going fine. I've put everything together for a test and did a ride - it was perfect! I disassembled it and solder nicely to hide and cut excess cables and now it is not working properly The engine makes strange sound and it does not rotate with full speed. Anyone knows what I did wrong? Here is the video:
https://www.youtube.com/watch?v=F3i3qrqHIBo&feature=youtu.be
The self learning procedure is not working properly - as it was before.
I'm building a commuter bike with q100c motor and a Chinese 17 amp controller with self learning procedure. The self learning procedure was not working for me. The engine always rotated backwards, but on the throttle it was going fine. I've put everything together for a test and did a ride - it was perfect! I disassembled it and solder nicely to hide and cut excess cables and now it is not working properly The engine makes strange sound and it does not rotate with full speed. Anyone knows what I did wrong? Here is the video:
https://www.youtube.com/watch?v=F3i3qrqHIBo&feature=youtu.be
The self learning procedure is not working properly - as it was before.