No, in the version I linked, the overrun is not yet solved.obcd said:Is this code already having the latest overrun fixes...
... do we have to wait a little longer for that?
You have to wait for the new version.
No, in the version I linked, the overrun is not yet solved.obcd said:Is this code already having the latest overrun fixes...
... do we have to wait a little longer for that?
Translation:chri27.5 said:Ciao a tutti,
Sto testando le ultime modifiche con Mbrusa, ci siamo quasi, bisogna aspettare ulteriori test per rendere definitive le modifiche.
Non ha senso rilasciare versioni che potrebbero causare problemi nell'utilizzo, spero che voi capite e pazientate ancora un pochino, vi posso assicurare che mbrusa è una grandissima persona e sta lavorando con passione e convinzione a migliorare il software per tutti voi.
Ciao chri27.5chri27.5 said:Hello to all,
I'm testing the latest changes with Mbrusa, we're almost there, we have to wait for further tests to make the changes final.
It makes no sense to release versions that could cause problems in use, I hope you understand and be patient a little longer, I can assure you that mbrusa is a great person and is working with passion and conviction to improve the software for all of you.
Elinx said:Ciao chri27.5
I can imagine that you don't want to release a complete new version of the firmware that isn't tested, but the question was if it is possible to publish the "overrun code" only from motor.c.
On Jobike I read this code could be used in the KT-lcd3 version too. In that case it is possible people ad this code by theirself and on their own responsibility.
Because mbrusa don't use github, we can't see the explicit changes with the code.
Thank you, mbrusa! :thumb:mbrusa said:this is the right one.
mbrusa said:motor.c file for open source TSDZ2 mb.20beta1.A for original displays VLCD5 VLCD6 XH18, with overrun modification.
..........
Thank you mbrusa. I tested it yesterday on about 5 km in central city, with the gear shift sensor on the way in and without it (unplugged) on the way back. It is hard to see huge differences now with an internal gear hub (I have a Nexus coaster brake 8 speed). It means that your improvements in order to shorten the overrun are very nice.mbrusa said:...this is the right one.
motor.c-TSDZ2-mb.20beta1.A-fix_overrun.zip
Walk assist isn't working with VLCD6.mbrusa said:A question to those who use the throttle.
Does it still work with fix overrun?
Thanks for the report, I had doubts about the throttle, but also the walk assist and the cruise are in the same conditions, the motor with the pedal stopped does not work. I will fix the bug and release the update later in the day.sp1n4d0 said:Walk assist isn't working with VLCD6.mbrusa said:A question to those who use the throttle.
Does it still work with fix overrun?
Thanks for your work, the motor it's running super smooth!
I've updated the github repo, it would be fine, if you would spend half an hour to learn how to use github! :wink:mbrusa said:Here is the "fix overrun" update in the TSDZ2-mb.20beta1.A version, for the original displays
Yes, now it's fine, thank you!mbrusa said:Here is the "fix overrun" update in the TSDZ2-mb.20beta1.A version, for the original displays.
The files to be replaced are 3, ebike_app.c, motor.c, motor.h
I had not considered the riding modes with stationary pedals, which consequently do not work.
Now "fix overrun" is disabled in WALK ASSIST, CRUISE, THROTTLE mode and for the next version also CADENCE SENSOR CALIBRATION MODE.
for sp1n4d0
Can you confirm the correct working? Thank you.
bingo5 said:In the same way the display (displaya data = 0) shows me 0.00 °C temperature.
My settings are:
#define ENABLE_THROTTLE 0
#define ENABLE_TEMPERATURE_LIMIT 1
mbrusa said:I attach the correct files, if you can update GitHub.